
But in my defence, the fuel gauge was showing 10.1 gallons! I am now wondering whether it has got a R21 fuel computer in it, which might not be calibrated correctly to the A610. I have the original computer - I know it was replaced at some point, so my next task will be to refit the original computer, but swap over the working display from the current one (I already did that job on my Quadra).
In taking a look at things, the garage found that one of the spark plug recesses was full of water - that would definitely be a contributory factor to the misfire. The top bleed screw wasn't done up tightly when I first got the car. Glad we found that!
Now looking forward to the next chapter! Aircon to be fixed next.
In other good news, my Gordini Turbo passed its MOT - first time back on the road in nearly three years! I fitted a 123-Tune electronic distributor, which should get rid of the issues I had with the old Renix ignition module (very conservative advance curve off boost, coil pack failures, etc.).